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Basic body parts for extruder |
I made the basic parts a while ago, without paying too much attention to how the extruder was supposed to be constructed and function. As a result, a few things are a touch suboptimal.
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Dremel 22m holes to fit bearings |
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Chamfer hole so motor sits flush |
The body is made of 5 layers. These are held together by bolts at the corners. Each layer is 9mm thick so the body is 45mm and I needed 50mm bolts to hold it together. Unfortunately I had already invested in a large box of M4 x 40mm socket cap bolts, so I looked for a way to manage with these slightly shorter screws.
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Countersinking M4 nuts |
I had drilled these holes 5mm in diameter, as shown on the plan; this resulted in an assembly that was excessively floppy with my 4mm diameter bolts, until they were fully tightened. I would have done better to check what bolts I had available and drill holes better adapted to their size, say 4.1mm.
I had planned to hobb an M8 bolt with partly smooth shank for the drive, but was unable to find a suitable one in the local (smallish) DIY shop. Plan B was to use an off-cut of the 8mm diameter steel rod we use in organ building, but this turned out to be some sort of hard tool steel (known in the french speaking workshop as stub, but this term resists my Google skills), and was entirely resistant to my efforts at hobbing.
I proceeded to Plan C. I cut a length of 8mm studding and arc welded a nut on the end. I then put the rod in a vertical drill and used a 3mm file (actually a chainsaw file) to cut a groove. The file needs a very firm support if it is not to be displaced by the thread, and of course you must work on the side of the rod which pushes the file towards the support.
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Cutting groove with a chainsaw file | Hobbing | The feeble result |
I used a 3mm tap in a cordless drill to actually cut the hobbing in the groove. I made jig out of a block of oak, with appropriately positioned holes to support the bolt and guide the tap against it. I regarded this as only partially successful. It was hard to position to holes accurately, the solid jig concealed the operation from view and did not allow the bolt to turn freely, and it did not provide a safe way to press the tap progressively closer to the bolt. I did succeed in cutting a light pattern, and would have attempted to do better, had I not snapped the tap while taking a photo one-handed.
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Countersinking the bolt head | Nice countersink, poor weld |
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Checking position of filament |
When tried assembling the parts, it was evident the slots in which the idler shaft slides were too short, and prevented the idler pushing against the filament. Also, that the bearing plus washer either side was thicker than the wooden layer they were supposed to fit into, and would prevent the layers either side from making proper contact.
A few minutes with file and dremel corrected both these problems.
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Putting the layers together |
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The assembled extruder |
I tested the grip of the hobbed bolt on PLA filament and found it better than I expected, given the shallow grooves I had made. On the other hand I am not at all sure that the springless adjustment of pressure will be adequate. Another problem is that the large gear extends too far down, and I will need to add extra spacers before I can fit it on the carriage.
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